Zakster87 Posted November 2, 2017 Share Posted November 2, 2017 Ported result. Think I took enough out? I did smooth it out a bit more after I took this. Still had to take a hammer to the jpipe as well. Did not clear the flapper whatsoever. Link to comment Share on other sites More sharing options...
Starks Posted November 2, 2017 Share Posted November 2, 2017 I'd clean up the bottom some more. As far as the hammer thing, before you did that we're you able to find the "sweet spot" where there's no interface or did yours not have it? Sent from my SM-G955U using Tapatalk Link to comment Share on other sites More sharing options...
Zakster87 Posted November 2, 2017 Share Posted November 2, 2017 It's got a pretty nice rounded edge on the leading side. Just really hard to get a good picture of it. I had NO sweet spot at all. the flapper could only open like 1/4" maybe. Tried orienting it forward or back, didnt seem to make a difference, still using stock studs as well. Link to comment Share on other sites More sharing options...
Starks Posted November 2, 2017 Share Posted November 2, 2017 It's got a pretty nice rounded edge on the leading side. Just really hard to get a good picture of it. I had NO sweet spot at all. the flapper could only open like 1/4" maybe. Tried orienting it forward or back, didnt seem to make a difference, still using stock studs as well.See, that's what I'm not liking. I'm about to add in an O2 bung on mine since it's already installed and thought about just removing the DP this time but I'm concerned about not finding that spot again when I put it back and end up having to take the whole thing off just to get it situated again. I would say some more about my dissatisfaction but I think it's been covered. Sent from my SM-G955U using Tapatalk Link to comment Share on other sites More sharing options...
GTEASER Posted December 12, 2017 Share Posted December 12, 2017 Just wanted to let everyone know that on a cold morning last week, maybe 35* out, my Fozz overboosted to 17.4 psi on the custom Stage1 tune that is targeted at 16. Stock TD04 turbo, stock catted DP, 2016 WRX OEM midpipe with Vibrant resonator and Nameless 5" muffled axlebacks. I have heard of other stock IHI turbos overboosting too, and now I have personal evidence. The TD04 is a tiny turbo, I just think that the overboost situation is more apparent and harder to control with the VF54. GTEASER's 2012 Legacy GT - Sold GTEASER's 2009 XTeaser - Sold GTEASER's 1992 Legacy SS - Sold Link to comment Share on other sites More sharing options...
ibr_adam09 Posted December 13, 2017 Share Posted December 13, 2017 Would it be safe to say that the Nameless downpipe performs just as well/ on par as other aftermarket catted down-pipes (regardless of what Nameless promised us and it's high price) if so, I'm fine with this. It's been sitting for awhile now and I've had urges to finally get the damn thing on haha. Link to comment Share on other sites More sharing options...
FLlegacy Posted December 13, 2017 Share Posted December 13, 2017 I think if you have a full exhaust you will get the most out of it, but don't expect to be amazed. You might also go ahead and port your exhaust housing if you haven't already. I am really thinking of getting the stock mufflers off right now...but I would probably need another retune. Then I was thinking I could change the timing belt, get some sti cams, and do the mufflers and get a retune...just rabbit hole after rabbit hole with this car. I also have it in the back of my mind to find a short block to build in my spare time, which is in the negatives right now...so much enabling to catch up with. Link to comment Share on other sites More sharing options...
BBPeik Posted December 13, 2017 Share Posted December 13, 2017 ^^^Funny, I have been thinking about picking up an extra block as well. It would be nice to have something to mess around with that does not need to get back on the road. Now the question is 3.6 or 2.5. hmmm My someday I will be done with it thread. Link to comment Share on other sites More sharing options...
Humble Rumble Posted December 13, 2017 Share Posted December 13, 2017 PLEASE build a 3.6 and mate an STi 6-speed to it. If anyone will do it right, it's you. I want to see what a proper build of that engine, WITH a manual, IN the car it was originally made for, so badly haha. 2012 Legacy 3.6R Build Thread 5th Gen Legacy BM/BR Body Kit Compendium Thread Link to comment Share on other sites More sharing options...
BBPeik Posted December 13, 2017 Share Posted December 13, 2017 That would be awesome. I would definitely add a turbo though. No snail no bueno. This is all a long way down the road, but I am sure my engine will blow up eventually. My someday I will be done with it thread. Link to comment Share on other sites More sharing options...
FLlegacy Posted December 13, 2017 Share Posted December 13, 2017 That would be awesome. I would definitely add a turbo though. No snail no bueno. This is all a long way down the road, but I am sure my engine will blow up eventually.Or a 3.0 you can build it with sti rods and pistons iirc. Sent from my SAMSUNG-SM-G920A using Tapatalk Link to comment Share on other sites More sharing options...
Starks Posted December 13, 2017 Share Posted December 13, 2017 What's up with all this spare block noise? Someone build a Super Gramps 5th Gen god damnit! Sent from my SM-G955U using Tapatalk Link to comment Share on other sites More sharing options...
GTEASER Posted December 13, 2017 Share Posted December 13, 2017 What's up with all this spare block noise? Someone build a Super Gramps 5th Gen god damnit! Sent from my SM-G955U using Tapatalk Do you care to make a donation to the effort in a large sum? I'll get right on that with the appropriate motivation. GTEASER's 2012 Legacy GT - Sold GTEASER's 2009 XTeaser - Sold GTEASER's 1992 Legacy SS - Sold Link to comment Share on other sites More sharing options...
FLlegacy Posted December 13, 2017 Share Posted December 13, 2017 Do you care to make a donation to the effort in a large sum? I'll get right on that with the appropriate motivation. Don't lie, you just want more parts to keep all your other parts company! Link to comment Share on other sites More sharing options...
foxrider28 Posted December 14, 2017 Share Posted December 14, 2017 That would be awesome. I would definitely add a turbo though. No snail no bueno. This is all a long way down the road, but I am sure my engine will blow up eventually.Why not twins? I mean it is almost 2018, anything with 2 headers has twins now. Of course I know how impractical it really is especially considering the stock space issues with the 3.6 Link to comment Share on other sites More sharing options...
BBPeik Posted December 14, 2017 Share Posted December 14, 2017 That would be awesome, but as you said finding the room would be tricky. Especially with that giant STI trans sitting in the way too. My someday I will be done with it thread. Link to comment Share on other sites More sharing options...
Starks Posted January 11, 2018 Share Posted January 11, 2018 Hate to bump this again but just letting you guys know I put down a deposit for my community's group tune at revworks/M-tune next Saturday. Between then I'm going to get this O2 bung welded in, nameless bpv on, and AEM dry flow in. So soon, we'll see what this thing is made of and if porting helped. Sent from my SM-G955U using Tapatalk Link to comment Share on other sites More sharing options...
Syndicate Posted January 14, 2018 Share Posted January 14, 2018 ...I'm dropping my LGT off for a pro-tune at IAG tomorrow, so I should have numbers around Weds or the weekend depending on when I can get back up there to pick up my ride. Link to comment Share on other sites More sharing options...
Syndicate Posted January 25, 2018 Share Posted January 25, 2018 (edited) ...so here are my final dyno numbers, 278whp and 350wtq. My tuner didn't make mention of any boost creep issues, so hopefully it stays that way. I'm hoping this will be a hoot to drive. Installed: AEM Dryflow air filterSamco inlet hosesAVO charge pipeGFB Mach II diverter valveGrimmspeed 3-port ECBSGrimmspeed TMICPorted wastegateNameless 3" downpipeInvidia 3" cat-back exhaust Edited January 25, 2018 by Syndicate Link to comment Share on other sites More sharing options...
GTEASER Posted January 25, 2018 Share Posted January 25, 2018 Wow! Nice! Any pics of the porting in the wastegate? GTEASER's 2012 Legacy GT - Sold GTEASER's 2009 XTeaser - Sold GTEASER's 1992 Legacy SS - Sold Link to comment Share on other sites More sharing options...
Syndicate Posted January 25, 2018 Share Posted January 25, 2018 Wow! Nice! Any pics of the porting in the wastegate? ...sure. Link to comment Share on other sites More sharing options...
Starks Posted January 25, 2018 Share Posted January 25, 2018 Happy for you! Glad your hard work paid off [emoji106] Sent from my SM-G955U using Tapatalk Link to comment Share on other sites More sharing options...
FLlegacy Posted January 25, 2018 Share Posted January 25, 2018 Happy for you! Glad your hard work paid off [emoji106] Sent from my SM-G955U using TapatalkHow did your tuning go? Sent from my SAMSUNG-SM-G920A using Tapatalk Link to comment Share on other sites More sharing options...
Starks Posted January 25, 2018 Share Posted January 25, 2018 Like ass! I was a victim of the nameless dp. I'll try and keep it short and sweet. Had a few boost issues. First they installed the GS ebc backwards, caused it to spool poorly, fixed that, then they did a smoke test because spool was still off, found a boost leak on the intake side of the intercooler. Fixed that. Then after while it would intermittently spool perfectly then spool like shit. Spent hours with the tuner trying to figure out what's going on and why I was peaking at 7 psi at some points and 18 at another. Long story short, the internal waste gate was getting hung on top of the dp's inlet from heat expansion. By that time it was late and about time to close. When I took that thing off prior to the tune date, I manually operated the flap for a good 2 minutes very carefully listening and feeling if it was touching. It wasn't, not until it heats up to a point I guess. So I have to take it off again and make sure it stops doing that. They cut me a break and said I can come back when it's resolved and complete the tune. We had the car on the lift, put some pressurized air in there and could barely just make out the arm sometimes binding and not. I am so upset with this piece. It's a big waste of time for a lot of people. It seems more like luck getting it in the perfect sweet spot than just following directions for an install. But we've discussed this all through this thread so there's no point in going back into it. I am going to get it into position or trim that lip or something. I'm going to get this to work. I intend on making my way back there early to mid February. Sent from my SM-G955U using Tapatalk Link to comment Share on other sites More sharing options...
FLlegacy Posted January 25, 2018 Share Posted January 25, 2018 Like ass! I was a victim of the nameless dp. I'll try and keep it short and sweet. Had a few boost issues. First they installed the GS ebc backwards, caused it to spool poorly, fixed that, then they did a smoke test because spool was still off, found a boost leak on the intake side of the intercooler. Fixed that. Then after while it would intermittently spool perfectly then spool like shit. Spent hours with the tuner trying to figure out what's going on and why I was peaking at 7 psi at some points and 18 at another. Long story short, the internal waste gate was getting hung on top of the dp's inlet from heat expansion. By that time it was late and about time to close. When I took that thing off prior to the tune date, I manually operated the flap for a good 2 minutes very carefully listening and feeling if it was touching. It wasn't, not until it heats up to a point I guess. So I have to take it off again and make sure it stops doing that. They cut me a break and said I can come back when it's resolved and complete the tune. We had the car on the lift, put some pressurized air in there and could barely just make out the arm sometimes binding and not. I am so upset with this piece. It's a big waste of time for a lot of people. It seems more like luck getting it in the perfect sweet spot than just following directions for an install. But we've discussed this all through this thread so there's no point in going back into it. I am going to get it into position or trim that lip or something. I'm going to get this to work. I intend on making my way back there early to mid February. Sent from my SM-G955U using TapatalkI smacked the side of the pipe with the hammer to make a slight flat spot right where the arm and flapper come open. I have had no issues with it. Kind of sucks but there is plenty of space inside the pipe for the turbine outlet. Sent from my SAMSUNG-SM-G920A using Tapatalk Link to comment Share on other sites More sharing options...
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