Klesseca Posted October 12, 2015 Share Posted October 12, 2015 Alright ill have to check that as well, maybe i should have done that gauge cluster...Hey well that explains it....lol thank you, there goes 120 bucks... lol Link to comment Share on other sites More sharing options...
Klesseca Posted October 12, 2015 Share Posted October 12, 2015 I noticed somthing very interesting from data mapping today on my way to and from work, the absolute tps % never exceeded 78% and also never dropped lower then 14% even at idle. Does anyone know the actual normal? I read other people have issues with tps and getting the same absolute % reading, if that's the case I may have just answered all of my problems..... Link to comment Share on other sites More sharing options...
StkmltS Posted October 13, 2015 Author Share Posted October 13, 2015 I'm pretty sure it'll never be at 0%, even at idle, because the ECU will always be giving the motor air and fuel. Even when you pedal-to-the-metal it doesn't show 100 %? Before you spend money on a new sensor I'd try to find somebody with a compatable car who's willing to swap sensors eith you for 2 minutes. While we're on the topic of logging... have you heard of BtSsm? Sent from inner space. My DiySB rebuild Got Misfires? Link to comment Share on other sites More sharing options...
Klesseca Posted October 13, 2015 Share Posted October 13, 2015 I actually just heard of it today and was doing the research, seems like it's worth every penny as I'm an android user. Yea on this forum there was another write up about tps, I believe idle is 5%, but wanna get stock specs. Just messing around I pulled the intercooler off and played with the throttle body, manual opening it all the way still only read 81% on ecm, and forcing all the way closed only 11%, it could make sensense if the send or is bad. But now after messing with the throttle body and unplugging it, as well as the petal, I have a constant code for that, that can't be cleared, and pressing the petal doesn't do anything (no throttle body control). Hmmm? Link to comment Share on other sites More sharing options...
StkmltS Posted October 13, 2015 Author Share Posted October 13, 2015 Sounds like something isn't plugged in all the way. My DiySB rebuild Got Misfires? Link to comment Share on other sites More sharing options...
Klesseca Posted October 13, 2015 Share Posted October 13, 2015 I disconnected both connectors again and made sure they were clean and locked in when plugged back in and still same issue no control Link to comment Share on other sites More sharing options...
heiche Posted October 13, 2015 Share Posted October 13, 2015 maybe disconnect battery for a few minutes and try again? BtSsm - Android app/Bluetooth adapter. LV, logging, gauges and more. For 05-14 Legacy (GT, 2.5, 3.0, 3.6), 02-14 WRX, 04-14 STi, 04-14 FXT, 05-09 OBXT Link to comment Share on other sites More sharing options...
Klesseca Posted October 14, 2015 Share Posted October 14, 2015 Tried that as well, with no luck Link to comment Share on other sites More sharing options...
heiche Posted October 14, 2015 Share Posted October 14, 2015 If you disconnect your throttle body and look inside the connectors, are any pins bent or mashed down? BtSsm - Android app/Bluetooth adapter. LV, logging, gauges and more. For 05-14 Legacy (GT, 2.5, 3.0, 3.6), 02-14 WRX, 04-14 STi, 04-14 FXT, 05-09 OBXT Link to comment Share on other sites More sharing options...
StkmltS Posted October 14, 2015 Author Share Posted October 14, 2015 MAF scaling is fun Finally I can do something to my car that makes a noticeable difference! My DiySB rebuild Got Misfires? Link to comment Share on other sites More sharing options...
Klesseca Posted October 15, 2015 Share Posted October 15, 2015 Nope made sure of that, disassembled everything again last night and cleaned the throttle body and electronic contacts on the pedal assembly, all while having the battery disconnected for a few hours. That did the trick, now have control of the throttle body again and no tb/pedaal codes. Still reading 16% closed and 78% wot Link to comment Share on other sites More sharing options...
SSpeed Posted October 19, 2015 Share Posted October 19, 2015 Good lord you stay the course!!! I would have pulled the motor by now just because it would have annoyed me so terribly. With all the work you've done, don't be scared of pulling the motor, sounds like it would be easy for you. Once you've done it once or twice it can be done literally in about two hours. Once out you can pull the heads and have the valves checked/refreshed and inspect the pistons if need be. If it is a burned valve you could pull the motor, send the heads off to be redone and have it back in the car in very little time. So much better than chasing down a ghost. And while you are at it you could do the things that are so annoying to do while in the car, like changing plugs, changing valve cover gaskets, oil pan, the oil filter o-ring, etc. Link to comment Share on other sites More sharing options...
xt2005bonbon Posted October 20, 2015 Share Posted October 20, 2015 Good lord you stay the course!!! I would have pulled the motor by now just because it would have annoyed me so terribly. With all the work you've done, don't be scared of pulling the motor, sounds like it would be easy for you. Once you've done it once or twice it can be done literally in about two hours. Once out you can pull the heads and have the valves checked/refreshed and inspect the pistons if need be. If it is a burned valve you could pull the motor, send the heads off to be redone and have it back in the car in very little time. So much better than chasing down a ghost. And while you are at it you could do the things that are so annoying to do while in the car, like changing plugs, changing valve cover gaskets, oil pan, the oil filter o-ring, etc. :whore: Link to comment Share on other sites More sharing options...
Klesseca Posted October 20, 2015 Share Posted October 20, 2015 Haha, yea the only issue is I refuse to pull the engine in a driveway and that's all I got right now, no garage unfortunately. I ordered a throttle body, and I'm hoping that is the issue, if not I will continue with leak down and compression test, which would also probably be a lot easier with the engine pulled.. Link to comment Share on other sites More sharing options...
StkmltS Posted October 20, 2015 Author Share Posted October 20, 2015 (edited) All in good time... all in good time. My wife and I will be out of debt (excluding the house) around Christmas, so my plan is to save up for a full-bore (get it?) #ynansb project next spring/summer. Thanks for the words of encouragement. This car was supposed to be a reliable replacement for my dying DD and it's grown into a project that's a little bigger than what I thought I was signing up for. It's been fun though and I'm happy for everything I've learned along the way. Edited October 20, 2015 by StkmltS My DiySB rebuild Got Misfires? Link to comment Share on other sites More sharing options...
StkmltS Posted November 6, 2015 Author Share Posted November 6, 2015 I just finished changing my timing belt, water pump, thermostat, and pulleys. I gave myself a little break from my general frustration with the car by painting the TB cover. Thoughts? The battery hasn't been connected for about a week and its refusing to start and showing the "ER IU" error again. Maybe when it isn't connected for a long period of time the IU fully drains and needs a little time to juice back up. http://images.tapatalk-cdn.com/15/11/05/91e5e03f4eb751c2ac217eb83987e7e7.jpg Sent from inner space. My DiySB rebuild Got Misfires? Link to comment Share on other sites More sharing options...
StkmltS Posted November 6, 2015 Author Share Posted November 6, 2015 The battery was measuring around 11.6 volts so I connected a portable jump starter (instead of the AC charger) and it started immediately. My battery is fairly new so I wonder why the voltage drops so much after being unused for only a week. Sent from inner space. My DiySB rebuild Got Misfires? Link to comment Share on other sites More sharing options...
xt2005bonbon Posted November 6, 2015 Share Posted November 6, 2015 Was the battery disconnected from the car for a week? If yes, voltage should not have dropped that much, unless it was already low to begin with? FWIW, this year when I worked on fixing my valve clearance issue, I took out the battery from the engine bay and did not use it for probably a good two months. When I plugged it back, car started right up. Battery is three years old. Link to comment Share on other sites More sharing options...
StkmltS Posted November 6, 2015 Author Share Posted November 6, 2015 Was the battery disconnected from the car for a week? If yes, voltage should not have dropped that much, unless it was already low to begin with? FWIW, this year when I worked on fixing my valve clearance issue, I took out the battery from the engine bay and did not use it for probably a good two months. When I plugged it back, car started right up. Battery is three years old. I left the battery in the car but the negative terminal was disconnected the whole time. After charging it overnight I still had to jump it this morning. It didn't even have enough power for the key fob to unlock the car. When I got to work and locked the car the alarm chirp was barely audible. I'm gonna take it back to Pep Boys and have it tested and hopefully replaced. There's no reason a 1-year old Bosch battery should act like this. My DiySB rebuild Got Misfires? Link to comment Share on other sites More sharing options...
xt2005bonbon Posted November 6, 2015 Share Posted November 6, 2015 I'm gonna take it back to Pep Boys and have it tested and hopefully replaced. There's no reason a 1-year old Bosch battery should act like this. Link to comment Share on other sites More sharing options...
StkmltS Posted November 9, 2015 Author Share Posted November 9, 2015 Every once in a while life hands you humbling situations to keep you grounded. The negative lead connecting to the battery was dirty. 'Er IU'/Voltage/starting problem resolved. I think I'm going to have my heads inspected/machined/cleaned/rebuilt as a separate project independent of getting a new SB. If my a bad valve is causing my misfire then my problem would be solved and I'd be a happy camper. If I still end up needing a full build then who cares, the heads would have gotten rebuilt anyways. Other than a catastrophic turbo failure I don't see any reason not to just do the heads. The best part is that it'll be easier to get my wife to sign off on it (because less $$$) , AND I can get my heads done in about 1/3 of the time It'll would take me to save up for a new block. This weekend I found out my friend has an '09 LGT that appears to be stage 2. The previous owner had all of the work done and my friend isn't very clear about what's been done to it. Driving it was a baaaaad idea because now mine feels so slow. I'm dying to see what my car would be like without a misfire. My DiySB rebuild Got Misfires? Link to comment Share on other sites More sharing options...
xt2005bonbon Posted November 9, 2015 Share Posted November 9, 2015 Yeah. Stage 2 is pretty nice. Well, if you get your heads rebuilt, you will at least be able to inspect the cylinder walls for scratches and stuff. Link to comment Share on other sites More sharing options...
heiche Posted November 9, 2015 Share Posted November 9, 2015 Every once in a while life hands you humbling situations to keep you grounded. Intentional pun? BtSsm - Android app/Bluetooth adapter. LV, logging, gauges and more. For 05-14 Legacy (GT, 2.5, 3.0, 3.6), 02-14 WRX, 04-14 STi, 04-14 FXT, 05-09 OBXT Link to comment Share on other sites More sharing options...
StkmltS Posted November 10, 2015 Author Share Posted November 10, 2015 Yeah. Stage 2 is pretty nice. Well, if you get your heads rebuilt, you will at least be able to inspect the cylinder walls for scratches and stuff. Yeah, and easy TGV deletes. Intentional pun? Haha I didn't even notice that, totally unintentional. My DiySB rebuild Got Misfires? Link to comment Share on other sites More sharing options...
StkmltS Posted November 18, 2015 Author Share Posted November 18, 2015 Puzzle of the day: Twice yesterday, for about 5 seconds of idling @ each stop, I heard and felt NO misfires. For the very first time since the problem started, I briefly felt zero misfires. What in the wide wide world of sports has the ability to cause/allow the misfire to temporarily stop? I ordered new gaskets and I'm going to delete my TGVs sometime in the next few weeks. My DiySB rebuild Got Misfires? Link to comment Share on other sites More sharing options...
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