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alex0856

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alex0856 last won the day on May 7

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  • Location
    Portland, OR
  • Car
    05 OBP LGT Wagon 5MT
  • Interests
    Wasting money
  • Occupation
    Fire Equipment Technician

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  1. So what you're saying is that the answer to all of my problems is a 6 speed? But yes it is adjustable. I break loose the nut and spin the bolt to tweak its positioning. No clue if this is the correct way to do it but since there's no instructions my options are limited I think what I'll do is pull the bolt all the way out, rock the car back and forth a bit and see where it rests. I remember that I initially torqued it down before I torqued the new cross member bushings, so my theory is that now that the rubber has been broken in a bit the car will let me know where it wants the mount to sit. Yesterday I drained my wallet some more. New clutch lines, BPV return hose, throttle body hose, and a Nameless BPV.
  2. You fancy people and your shiny cars, what with their clear coat, door panels, and sub-100k odometers...meanwhile I'm over here feeling good about not having my shifter surround rolling around on the floor anymore. I've lost count of how many times I've torn it apart and it shows. Since my foam shifter insulator was falling apart, I constructed a new one from luxury liner pro. Between that and the deadening on the transmission tunnel, I can hardly hear that classic subaru 5MT whine. Now my cabin is officially reassembled and I can truly enjoy the silence. I'll have to stop myself from ripping off the door panels to get those insulated as there are much bigger fish to fry. I pulled the intercooler off yesterday and checked some hose clamps, tightened the galvanized plug on the back of the intake manifold, and adjusted the pitch stop. My idle is better now but not perfect. I ordered some pipe plug sockets to properly snug up that plug as I think it may have been a huge contributor to my rough idle. @KZJonny I have learned to despise worm clamps. I've got so many in my engine bay now and it takes 3 different nut drivers and a flat head to operate them. I've got them positioned to be mostly accessible but some are very buried in there now. They also destroy hoses IMO. I just spent $85 on a new BPV return hose because the clamp took a chunk out of my venair hose. Can anyone advise on pitch stop adjustment? My OEM is only 6 months old and I'm having a hard time finding the best positioning. The FSM doesn't appear to have any adjustment instructions. It just says to adjust. Yesterday I centered it on the bean shaped hole on the trans bracket and now the car bucks like a horse when you let off the throttle. Not interested in a stiffer one, I'm trying to keep my car as soft as possible.
  3. These are a godsend https://www.harborfreight.com/3-piece-long-reach-hose-grip-pliers-37909.html Makes me think that the tech fought and fought and fought the hose, chewed it up in the process, then said "oh well".
  4. Found the problem When I pulled my trans I opted for the Neanderthal method - position a cart with wooden blocks to support the trans, then use the lift to bring the car and trans to the blocks. Works fine for getting it off, I guess, but I went and bought a transmission jack after this experience because I'm an adult. I very brilliantly forgot to support the engine when we did this, and found it being held up by the main wiring harness and fuel lines - awesome! The delivery and return lines moved a good inch, but appeared to survive. I just noticed today though that the return hard line has a nice kink in it. This is after I bent it back a bit. I guess my problem could be other things, but I can't imagine that it's very happy with me for doing this. The soft lines ("dampers" as subaru calls them) are either $87 or discontinued. Fortunately I dug up a helpful comment by some guy named Infosecdad from 2017 with Dorman part numbers to build my own.
  5. I'm glad I replaced mine when I did my clutch - turns out it's not so bad when there's no transmission in the car. In fact, I think I'll just go ahead and pull the trans next time I need to replace that hose. It'll be less of a headache. I have a couple of the OEM hoses on hand and I swap a new one in every time the turbo comes out. If I'm replacing it with the turbo still bolted down, I'll pull the downpipe as that only takes a few minutes and gives you a lot more room. I have found that the best approach is to cut the old hose out, heat gun the new one a bit to make it softer, apply a tiny bit of grease to both ends, then slide it on to the turbo. Drop your clamps over the crankcase drain, then grab your trusty hose clamp pliers and twist it back and forth until it makes contact with the lower drain. Then I use my industrial grade persuasion tool (big ass screwdriver) to push on the hose while I continue to twist until it slides fully over the drain. Lastly, I take the hose clamp pliers and pull down on the hose from the top, being careful not to marr up the hard line. @killjoy323232 sounds to me like they used a generic hose that wasn't rated to both carry oil and live in the hottest part of the engine bay. Bums me out when "professionals" can't figure out those simple things.
  6. The car is finally home. There's still much to do so for now it's being limited to grocery store trips (its favorite activity). The intermittent FKC is driving me crazy. From my limited knowledge on knock corrections, the inconsistency of it is why I haven't taken any hits to FLKC and IAM. It's difficult to replicate the problem and I find I can only do it in situations where you wouldn't expect the car to be yelling "woah there partner" at me. WOT though? Happy as a clam. My smoke tester is showing up today so I'll give that a shot. Once the boost leak tester arrives and I can rule that out as well (assuming there are any problems), I'll move to the parts dartboard. The high pitched "sp sp sp" noise I hear under heavy boost has to be some form of malfunction. I should really try to find my missing 8mm socket. I couldn't find it on top of the block but maybe it's just hiding.
  7. Today I ordered some misc vacuum system parts and extra gaskets since I blew through my stash last month. I really need to build a parts shelf in my garage. I have no clue if I'll see any benefits from replacing my EVAP purge valve but I figure it's a 20 year old plastic moving part that lives on top of an engine block, so you'd think it wouldn't be performing like it used to. I also bit the bullet on a new OE o2 sensor since I'm sure mine is fried. Has anyone used the Torque Solutions boost leak tester? I'll be purchasing a boost leak tester and possibly a smoke tester soon just to rule out the easy stuff before I start throwing parts at it. I haven't ordered it yet though because I keep forgetting to send a whiny email to RSD to complain about my crappy throttle body hose that I gave up on trying to fit. My mishimoto doesn't appear to have holes in it but the outside layer is flaking off and I can see the webbing under the silicon. The next thing will probably be a BPV because again, 20 year old plastic moving part. Tomorrow I'll hit the private race track that I definitely have for some data logging and make a post. I'd like to get other's opinions on if this is a fuel issue or an air issue. I'm highly confused by the beautiful LV but random huge fuel and timing corrections. And the psst noise.
  8. Oops, I posted that when I was falling asleep. I added a screenshot I took after doing some runs on my private race track. There were a few fuel correction and knock events but surprisingly nothing hit the LV. I saw that FKC gauge max out just by tapping the accelerator at 70mph in 5th. But at WOT it would be at 0.
  9. My car is finished! Sort of. I actually started it on Sunday, and was greeted by a rough idle. Found some connections that I forgot to tighten or didn't tighten enough and it improved. Since I'm on a 12 day work streak I didn't have a chance to touch the car again until tonight. Giving the plastic drain on the AOS another spin and tightening up the rocker cover breather hoses seems to have eliminated the rough idle. However it's not perfect. I'm just glad to be rid of the garbage PCV. What I am finding is that a problem that existed when I first got the car running again is still present, but improved. I think I have a vacuum leak, or something mechanically is wrong with the vacuum system. If you just tap the throttle from idle, you'll feel a shudder between 800-1100 rpm. Same goes for holding it in those ranges. Then it clears right up. If you rail on the car, it actually performs better. BUT, you can hear a high pitched sputtering sound under heavy boost. According to btssm I'm hitting 18.4psi, but I'm fairly confident we only ever tuned for 17. Or maybe it was 19? Who knows. All I know is that something is off. In this process I've removed the PCV valve system, replaced most of the vacuum lines, turbo inlet, intercooler to TB hose, BPV and intercooler gaskets. I found one hell of a clog inside the OEM crossover pipe that connects the rocker cover breathers. I chopped it up so I could still use it to secure the main wiring harness. My LV is an improvement but we're maxing out fuel correction on hard pulls and getting highly inconsistent knock correction. I even managed to generate a misfire on a WOT pull. I've attached screenshots I took while running tests on my private track in my backyard. My mechanical brain is telling me that the issue is with a moving part. A leaking BPV makes sense but I can't confirm. In the mean time I will be getting it home and driving easy. I'm likely going to purchase tools to check for vacuum and boost leaks. If that checks out then I'll start throwing parts at it. On a positive note, the clutch and trans are like butter. I can't believe how much of a difference replacing my shifter components made. That combined with rack bushings means it handles like a new car now.
  10. Getting very very close. And feeling grateful for kind and patient friends. I had been hoping to be able to drive the car to my grandfather's interment yesterday but it just wasn't in the cards. He always liked my car and always had fast and impractical cars himself. I wish I would have had the chance to take him for a ride in it, but that's okay. A word of advice to all - call your grandparents/parents/elderly friends and relatives today. They've simultaneously got lots of time and limited time, and they'd love to hear from you. Back to business - The trans and driveshaft are in, with new bushings to boot. My subframe was like a wet noodle before (I pulled it off the trans in one piece) but now it's much firmer. I'm expecting a solid improvement in handling. Tonight I blew 3 hours trying to replace a CV axle boot that I accidentally tore. Unfortunately an OE boot would not fit my aftermarket axle so I decided to fill the small tear with gray gasket maker for now. Since I've got two new boots I'll probably hit pick N pull for an axle and rebuild it. The inlet and AOS are all set, just need to make connections and decide on how I'm going to reroute the wiring harness. Question for all - does your shift linkage have this much play between the washer and trans bracket? I had lightly sanded mine before reinstalling to remove some built up surface rust. My bushings fit snugly in to the linkage itself but I've got this gap and can't say if it was there before. The linkage has about 2mm of lateral play. The bushings are almost new. If that's supposed to be solid then I suppose I'll buy a new one.
  11. Never. After this go round of remodeling there will be very few plastic and rubber pieces left to replace. When I did my suspension and brake overhaul it felt like a brand new car. I'm expecting it to drive like a dream. Also, I'm in way too deep at this point. Sunk cost isn't a fallacy in this context, it's a way of life.
  12. The trans is ready to go in. Replacing the oil seal on the linkage was pretty annoying but I got it without damaging anything. I attempted the screw trick but there's just not enough meat to get a proper bite without risking marring up the linkage or housing. I found that a heat gun, a shaved down pick, and patience was the way to go. Last night I put in new rack bushings, shifter joint, trans mount bushings, and tore down my short shifter. The bushings are pretty new but the metal needed cleaning and the grommet that goes on the tunnel badly needed replacing. I didn't expect to be able to get that part new but it turns out Subaru still uses it in other cars. Go figure. I'm on the road for work today so no shop time tonight. Tomorrow everything should be coming together.
  13. Being a car person is a bummer sometimes. I should sell it and buy an automatic Corolla. My car still isn't done unfortunately. A mixture of the "while we're here" curse and finding more problems has dragged it out quite a bit. The trans is sitting on the jack ready to go with a new fork, spring, and pivot ball, and the clutch is installed. I drained the coolant to pull the turbo because reasons and found the lower oil drain was crushed - probably from 22 year old me using channel locks on it. It wasn't causing a restriction from what I can tell, it was just oval shaped and causing a leak. Fortunately you can buy replacements still. Today I'll finish getting the perrin inlet installed, then the AOS and rack bushings. I might even get the boot swapped on my year old CV that somehow got a hole in it. While swapping my heater hoses and pulling the upper rad hose I found what appeared to be coolant seeps, likely from the car sitting for so long. I think I've got contamination in the system as well. I'll probably do some sort of flush once it's on the ground. Hopefully my shift linkage seal and turbo oil drain will be here by Tuesday. I'm supposed to be driving it to Seattle next weekend. I think the problem all along was misalignment caused by dumb kids replacing a clutch without the proper tools. Here's some pics of the gore. You can see where the clutch disk was only partially grabbing. I wish I had got one of my bell housing before I cleaned it out. The ring on the back of the flywheel was from a nut that fell in to my bell housing and landed perfectly behind the flywheel. I'll have to find it and take a pic. It's got nice char marks on the head. I'm glad I bought a new timing inspection cover.
  14. I have wanted one for a long time but you can't buy them new anymore unfortunately. I'll probably end up going aftermarket at some point.
  15. Oh definitely. He has told me this himself. I find myself feeling self conscious about using his lift every time I ask. So I help him with his projects whenever I can. He's been working on scrapping a WRX for a while now which was tied up on the lift so we spent a Saturday stripping it so it can be hauled off. Although I won't lie, I found dismantling a car that I didn't need to put back together a lot of fun.
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